FAA Incident Report - Mar 2009
Author: Lectromec
Published: 09-01-2009
FAA's
Reported Wire Incidents – March 2009
Author:
Lectromec GSD Team
August 23, 2009
The
following are the wire incidents reported in the FAA’s March
2009 Advisory Circular 43-16A – Alert Number 368 [Original
Document Here]
http://www.faa.gov/aircraft/safety/alerts/aviation_maintenance/media/2009/2009_03_Alert.pdf
Incident
# 1
Aircraft
Make: Cessna
Aircraft
Model: A150K
Part
Name: Air Intake
Part
Condition: Water Block
A
mechanic provides this excellent analysis of his customer's aircraft
problems. "The owner took off for some pattern work. (Since...)
the weather had been cold and clear for several days he thought
it perfect for touch-&-goes. On the downwind leg he began his
normal landing check list—including checking the carburetor
heat. After pulling (this heat control) 'ON' the engine died.
He turned off carburetor heat and the engine restarted on its own
without pilot input. He continued the pattern and gradually reapplied
carburetor heat on base and final. On short final the engine died and
the pilot glided to a safe touchdown just beyond the end of the
runway. He was able to restart the engine and taxi back to parking
without incident. We looked at the engine...and found the Scat hose
(model 150 & A150; 1970-77 parts manual; figure 56; sheet 2; item
29) coming from the front baffle down to the front of the exhaust
shroud had filled with water. The installed hose is in the form of a
'J', and the bottom of this 'J' was full of water and ice. In our
damp climate we have noticed this before and usually ensure each scat
hose has a drain hole in any low areas. Somehow this (particular)
aircraft had been missed. We have found water and ice in similar
installations on Cessna 150 and 172 series aircraft. Because of their
location, the air intake scoops in the front baffle funnel rain water
into the SCAT hose, (filling) the forward hose. Sometimes the
water overflows the front hose and flows along the lower inside of
the heater shroud, (attempting...) to also fill the carburetor
heat box-to-right-shroud Scat hose (model 150 & A150; 1970-77
parts manual; figure 56; sheet 2; item 19). This results in the
engine receiving a large slug of water or ice when the carburetor
heat is applied. Whether the water is in a liquid or solid form
depends on the duration of the flight and whether the heat of the
operating engine has melted any ice that may have formed during
periods of inactivity. This is a dangerous condition during weather
conditions when carburetor icing is a possibility. The pilot would
(be prompted) to turn on the carburetor heat to clear any
icing that may have formed through the normal induction system.
Instead of getting warm air as expected, the engine would suddenly
receive a small to very large burst of water or ice into the
induction system that could instantly refreeze, plugging the
induction system entirely. So far, we have not seen this happen. We
normally encounter this problem in warmer months when we receive more
rain. Under those conditions the pilots notice a rough running engine
when carburetor heat is applied, and turn the heat off before the
water is fully removed—or (they opt) to continue with
the heat (applied and the resulting engine roughness...)—until
the water clears from the hose. One way to check for this problem on
any aircraft is to (examine) the scat tube reinforcing wire
for rust in the lower areas. The occasional water build-up will cause
these reinforcing wires to have more pronounced rust on the lower
portions where water would sit on the wire wraps. Any aircraft
showing abnormal wire deterioration in those areas should consider
installing drain holes.
Incident
# 2
Aircraft
Make: Piper
Aircraft
Model: PA31-350
Part
Name: Fuel Pump
Part
Condition: Electrical Failure
An unidentified
mechanic relates the following description. "(The aircraft
was departing the field...) when he reported he lost substantial
power to the left engine just after take off, and that the left low
pressure fuel boost pump light on the aircraft annunciator panel
illuminated. He (effected a safe landing at an airport) and
called for aircraft maintenance. The aircraft technician on location
could not find any problems with the engine during run-up other than
the electric, low pressure fuel boost pump not supplying rated
pressure. (Note: the electric, in-line low pressure boost pump is
intended for flight above 15,000 feet MSL and can be deferred, as per
our Part 91 MEL (minimum equipment list). The aircraft
(initiated its take-off roll for departure...) when the left
engine again lost power at (approximately) 40 knots airspeed.
(Subsequent) trouble shooting of the engine fuel pump and fuel
nozzles revealed no problems. The in-line low pressure fuel pump was
removed (revealing) the bypass valve assembly in the pump had
dislodged from the pump body and acted as a fuel (flow)
restriction to the emergency electric fuel pump. We have been
operating the Piper Navajo Chieftain aircraft for 20 years and have
never seen this happen until now."
(Parker
Hannifin Pump, P/N 2B6-64. Time since overhaul: 2,098.4 hours. The
FAA Service Difficulty Reporting System (SDRS) reflects 11 entries
for this part number.)
Incident
# 3
Aircraft
Make: Piper
Aircraft
Model: PA32R-301T
Part
Name: Main Gear Down-Lock Switch
Part
Condition: Failing
(The
following combines five reports on four PA32 aircraft—all from
the same mechanic.)
This aircraft's
"...main gear down lock switch wires pull tight on the strut
during retraction, pulling wire strands apart to the breaking point.
The silicone type wire coating tends to hold the wire ends together,
creating intermittent contact. (This assembly) needs better
wire and routing."
Incident
# 4
Aircraft
Make:
Aircraft
Model:
Part
Name: Wire Harness
Part
Condition: Frayed
Part
Location: NLG
Nose Landing Gear
electrical harness - outer fabric shield - frayed. Harness replaced.
Incident
# 5
Aircraft
Make: Airbus
Aircraft
Model: A310304
Part
Name: Wire
Part
Condition: Arced
Part
Location: Fusleage
Mechanic noticed
flash of light from left wheel well. Found power supply wire bundle
under support clamp on aft wall of left wheel well. System was
deactivated and put on MEL 29-2. Harness will be replaced at the next
available downtime and harness will be routed to engineering for
evaluation. (TC NR 20090112009)
Incident
# 6
Aircraft
Make: AMD
Aircraft
Model: Falcon
Part
Name: Power Supply
Part
Condition: Defective
Part
Location: Cabin
Wrong parts inside
strobe power supply PN 39-44-31: C3, C6, C9 (capacitors), Q5
(transistor) and wire color. No serial number on unit; serial number
on customer paperwork is 1024088873.
Incident
# 7
Aircraft
Make: Beech
Aircraft
Model: B200
Part
Name: Wire
Part
Condition: Broken
Part
Location: Reset Switch
Air conditioning
reset switch located in the wheel well found broken. Upon examination
of switch it was noted factory installed heat shrink tubing was not
properly installed thereby allowing it to migrate away from the
switch connector. This in turn caused exposed electrical wiring which
given the right conditions could cause electrical arcing and possibly
smoke and/or fire. This defect was discovered as a result of normal
inspection however review of previous discrepancies showed this was
not the first occurrence of failure for this switch installation.
Stores inventory was checked and found spares had the same flaw.
Before installing new switch, additional heat shrink tubing was
installed illuminating the possibility of further occurrence. (TC NR
20090126005)
Incident
# 8
Aircraft
Make: Armgen
Aircraft
Model: AA5B
Part
Name: Wire
Part
Condition: Burned
Part
Location: Beacon
During annual
inspection flashing beacon was found to be not working. Upon tracing
the wiring a burned wire was discovered at junction jp-1-2 below
instrument panel aft of center console. This was the second time that
burned wires were found at this location on this type of aircraft and
the third time that burned wires were found at a connector in the
flashing beacon circuit.
Incident
# 9
Aircraft
Make: Boeing
Aircraft
Model: 777*
Part
Name: Wire Harness
Part
Condition: Worn
Part
Location:NR 2 Engine
On NR 2 engine found
harness W729 damaged behind fan cowl at 6 o’clock position. The
damage was caused by the harness rubbing on each other. The harness
was changed and repositioned (TC NR 20090115001).
Incident # 10
Aircraft
Make: Boeing
Aircraft
Model: 777*
Part
Name: Wire Harness
Part
Condition: Worn
Part
Location: NR 1 Engine
On nr1 engine found
harness W721 damaged behind fan cowl at 8 o’clock position. The
harness damage was caused by the rub between 2 electrical harnesses
W721 harness replaced and repositioned IAW B-777 AMM task
70-00-01-400-806-H-01. (TC NR 20090115002)
Incident
# 11
Aircraft
Make: Bombardier
Aircraft
Model: BD1001A10
Part
Name: Generator
Part
Condition: Fire
Part
Location: APU
After
APU start at fl100 just before APU gen on line APU fire CAS message
posted. Pilots arm APU bottle message disappeared. Pilots shutdown
APU and land a/c safely. In aft equipment bay pilots noted an odor of
burned wire. After inspection of APU generator found generator on
fire. Fire went out via cooling duct to educator sensing element of
APU fire detection system. APU door showing signs of fire.
Incident
# 12
Aircraft
Make: Cessna
Aircraft
Model: 182P
Part
Name: Connector
Part
Condition: Burned
Part
Location: Light Switch
Pilot reported smoke
in cockpit after takeoff and returned to the airport making an
uneventful landing. Maintenance inspected the aircraft and found a
loose connection at the landing light switch with burned wiring
insulation. Installed new wiring and connector as needed and ops
checked good. Push-on type of wiring connectors need to be checked
closely for security during scheduled maintenance.
Incident # 13
Aircraft
Make: Cessna
Aircraft
Model: 208
Part
Name: Wire
Part
Condition: Burned
Part
Location: Prop Deice
During inspection it
was found that the electrical connector and approx 3 inch of wire
forward of the vanister. In the prop de-ice CCT was burned and the
wire had become separated from the Vaniston leaving the prop de-ice
system in-active. Flight crew was unaware of any inoperative systems.
Wiring was repaired and connector replaced, system function tested
normal. Submitter suspects/connector wire had worked loose over time
causing arcing/burning with wire finally fell off. (TC NR
20081222005)
Incident
# 14
Aircraft
Make: Cessna
Aircraft
Model: 208B
Part
Name: Wire
Part
Condition: Chafed
Part
Location: Tail Beacon
The pilot reported
his tail beacon inoperative. Maintenance techs troubleshot the wiring
and found that the wiring bundle that contains the power wire for the
tail beacon where it routes over the glove box had chafed on the
glove box. The chafing caused the wire to burn through the glove box.
Incident
# 15
Aircraft
Make: Canadair
Aircraft
Model: CL6002B19
Part
Name: Sensor
Part
Condition:Malfunctioned
Part
Location: Brake Position
Flap fail on descent
when flaps set to 45 deg. Oat was 3 deg. Crew indicated that flaps
failed appeared after flaps had reached 45 deg in both event. Action
plan 156-jan-4-09-plan 2 c/out, left BPSU replaced IAW aircraft mm
27-51-10-830-801, left BPSU wiring checked no fault found.
Incident # 16
Aircraft
Make: Canadair
Aircraft
Model: CL6002B19
Part
Name: Actuator
Part
Condition: Malfunctioned
Part
Location: TE Flap
On
final approach, crew selected flaps to 45 degrees. Flaps failed at 38
degree. Forecast oat at altitude was -60C. Oat at landing was - 2
degree. No emergency was declared and flight landed safely. Aircraft
had been in flight for about 2 hours. After landing crew positioned
flap lever to 0° but there was no movement of flaps. Maintenance
received the following fault codes from the FECU: 1. Jam. 2. Left
BPSU. 3. Wiring left BPSU. An action plan was developed for
lubrication and freeze checks of the left actuators. NR 3 and NR 4
left actuators failed freeze check. Maximum breakout torque is 15 lb
in, reading for left NR 3 was 27 lb in and left NR 4 was off the
scale. Per these findings a second action plan has been issued to
replace all 8 flap actuators. Removed actuators to be sent to vendor
as a ship set for further investigation. It was noted that this set
of actuators had only recently been installed (TSR 98 hours) and all
were the upgraded version of actuator. (TC NR 20090107003)
Incident
# 17
Aircraft
Make: Canadair
Aircraft
Model: CL6002B19
Part
Name: BPSU
Part
Condition: Failed
Part
Location: TE Flaps
During final segment
of climb, the flight crew received a flap fail message on EICAS. The
flaps were at zero and were indicating zero at the time. The QRH was
followed and the aircraft landed without incident. Maintenance
checked FECU for fault codes and found codes for right BPSU, FECU and
wiring for right BPSU. The system was reset, the flaps were ops
checked and no further defects noted. Aircraft returned to service.
In cruise flight, the flight crew received a flap fail msg. The
flight control synoptic page indicated the flaps were outlined in
yellow showing zero degrees of extension. The aircraft landed back
without incident. Maintenance pulled FECU codes (see attached) which
indicated right BPSU or wiring. The right BPSU was replaced, the flap
system was ops checked and no further defects noted. Aircraft
returned to service.
Incident # 18
Aircraft
Make: Bombardier
Aircraft
Model: DHC8102
Part
Name: Generator
Part
Condition: Malfunctioned
Part
Location: NR 1 AC
Shortly after take
off, the flight crew received "NR 1 AC gen" and "NR 2
AC gen" caution lights. Systems were reset and NR 2 AC
generator returned on line. Decision was made to return and the
aircraft landed without further incident. The NR 1 AC generator was
replaced and the phase A and C wires located under the right flap
between the nacelle and the fuselage were repaired. Both wires were
shorted due to chafing.
Incident
# 19
Aircraft
Make: Embraer
Aircraft
Model: EMB145LR
Part
Name: Wire
Part
Condition: Chafed
Part
Location: RT Nacelle
IAH - flight 2749,
the crew reported the NR 2 engine fire detection system failed in
flight. The aircraft returned to IAH where it landed without
incident. Maintenance inspected the aircraft, and repaired wires
W407-0011-20 & W407-0012-20 near connector P0914, ops checked
with no defects, and the aircraft was approved for return to service.
Incident
# 20
Aircraft
Make: Swearingen
Aircraft
Model: SA226TC
Part
Name: Solenoid Valve
Part
Condition: Mismanufactured
Maintenance replaced
the bleed air valve solenoid for a flight snag. The PN320250-4-1
solenoid is located in the right WW of the aircraft. After
replacement of the valve the AME did not notice that the electrical
connection for the cannon connector on the valve was oriented
differently than the previous valve which was removed. The wire
harness and connector was able to be hooked up in this different
configuration. Normally with the valve installed, looking forward the
connector in at a 2 o’clock position. This replacement valve
has the connector located at approximately the 6 o’clock
position. The aircraft was dispatched and after takeoff the crew
retracted the gear and noticed the right main landing gear remained
in transit rather than locking in the up position. The gear was
recycled with no success. The crew elected to return to the airport
and landed without further problems. Maintenance immediately noticed
that the nr 3 tire had markings on it from contacting the bleed air
solenoid connector when it was attempted to be retracted. This
damaged the valve bracket and the connector, the valve was not
damaged. Maintenance realigned the cannon connector and reinstalled
the valve with a new bracket, performed a gear swing and released the
aircraft.